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Akira Bike
by: Evilgenius - Apr 16, 2012 17:42:59 GMT -6
Post by Evilgenius on Apr 16, 2012 17:42:59 GMT -6
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Post by Evilgenius on Apr 7, 2012 16:13:15 GMT -6
A bit posthumus, as this was from a purchase back near the end of February, but hopefully no less relevant. For what was intended to be a wintertime upgrade (having no clue of the unseasonable warmth to come), I ordered several things from the Mainely Scooters eShop: - 15/38 Final Reduction Gear Set (NCY)
- Dr. Pulley sliders (11g)
- 2x Kenda K413 Tires, 130~120/70-12
- Gearbox gasket
- Iridium Plug
- Gates Powerlink 842 belt
- Exhaust gasket
Checkout was not a problem. Communication was good, with a total of 4 update emails as the order processed and shipped. This reflected well on expediency, as the order was prepped and shipped over the course of about 8 hours on the same business day. I ordered things from several vendors online that day, with this order arriving first out of about 4, so shipping was PDQ. Considering I was about 1/2 way across the country and said shipping was also free, not bad at all. Packaging was secure and professionally labeled - adequate for reasonable protection of the contents (there was the inevitable smushed corner by the shipper on this fairly sizable box, but nothing damaged inside). Without drifting into product reviews, I was pretty satisfied with this vendor. Pricing was very fair IMO - when all was said and done, I paid slightly less for quality, branded stuff than I would have paid for questionable-quality generics of similar function from some other sources, so that's about as much as one could ask for in my book. Will definitely be looking back to this vendor for future orders. The information presented here is the unverified experience of Evilgenius and may not necessarily reflect the views and opinions of staff, management, and/or your crazy neighbor lady's pet parakeet. "Believe it or not."
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Post by Evilgenius on Feb 13, 2012 16:59:41 GMT -6
Thanks, JB. I did think to give the Norton-neutral disclaimer, but didn't consider the ramifications of oil selection, a fiercely-debated topic. Good to see fellow Kentuckian, BTW! ;D Looks like Havoline got hoovered up into Chevron back in '01, JR. For now at least, Havoline dino looks to still be widely available, but eeple say the Havoline synth is scarcer than chicken lips at this point. The site claims it still exists, but I'd bet the formula either evolved into something else, or is 'canned' from the market in favor of some competing Chevron product (Delo variants being the primary suspects in either case). Even Google can't find any!
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Post by Evilgenius on Feb 9, 2012 22:29:58 GMT -6
...how am I gonna get this on my scooter?! Gonna have to break out the extra bungee cords on this one... ;D
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Post by Evilgenius on Feb 9, 2012 20:01:21 GMT -6
;D
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Post by Evilgenius on Feb 9, 2012 19:25:07 GMT -6
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Post by Evilgenius on Feb 7, 2012 21:21:00 GMT -6
*sigh* ... they've all gone absolutely effing mad over there... +1 ex-dawg.
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Post by Evilgenius on Jan 14, 2012 10:54:52 GMT -6
I have an '07 Lifan, that was built to '06 spec. The engine itself has been very solid. Rubbers and plastics are suspect due to age at this point. If it's been well-kept, in good running condition, at a good price, and you're capable of some replacing of hoses & such, it might be an option. My opinion of Lifan in regards to a lot of other Chinese scoots is a bit higher. Lifan does make cars too, so that would seem to imply some manufacturing capability there. Whether it is or not is anyone's guess. So...a positive opinion on Lifan scoots of the same approximate age, but I'm with JR on this one: more details, please!
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Post by Evilgenius on Sept 30, 2011 16:15:29 GMT -6
Woke up to calm winds and mid-50's. Schweeeeet. Started right up, idle sounded good. I could tell pull was greatly improved before even leaving my street. Sure enough, power has been restored to approximate previous levels throughout throttle range, if not better in some. Low end oomph seems noticeably better. Not "hold on to your teeth" better, or anything, but it's there. :-XI think it was just starving before. Midrange maybe a little more than previous. WOT maybe slightly less on top speed than before, but holds speed more securely; less rickety-feeling and more solid. "Roadworthiness +1", if you will. All things pointing to the previous setup being a smidge too lean. That, and the paint on my header pipe hasn't chalked up yet, so I'm calling it a win by both counts. Idle sounded *exactly* as it should be after the run, which is also a good indicator. Speaking of sound...I gotta say that the straight filter intake to carb is waaaaay louder than either the opened airbox, or the (unfortunately restrictive, but still very cool) PVC setup. When the visor's shut, I really don't even hear the muffler for the intake now. A future trip to Lowe's will likely find me coming home with a similarly constructed but larger I.D.'ed intake contraption, when I have access to a wider range of random fittings. Can't help but think she still would like a little more air, though. It's close enough, but perhaps the Emgo will be less restrictive when it arrives. The seasonal swing in temps will favor leanness too, so I'm guessing this is right about where I need to be for now anyway. I will likely be looking into your muffler recommendations after the dust settles, JR. I am unfortunately not weld-capable, so going larger on the pigtail isn't an option. I might very well try the secondary holes in the back wall of the outer chamber and see what kind of results I get either using the opened holes, or by plugging one/both of them. Sounds like good material for a future thread, even. ;D
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Post by Evilgenius on Sept 29, 2011 21:41:29 GMT -6
Hee hee...I was wondering when you'd show up JR! ;D Was hoping to get your input. What's that you say? "Go another step?" Don't mind if I do! Well, I upped the clip one notch, and that's as far as it goes. Might theoretically get a little more adjustment out of it by swapping the plastic needle shim for a washer, but I'll just get another jet before that. Still stumbling mid-range, but in the cooler air, WOT was feeling pretty good. Well enough to cruise a couple miles on the highway. So I'm thinking: why so much problem choking down this seemingly paltry amount of fuel? It's only a 38/115 jet set, on a crappy but very free-flowing filter. Upon further examination, I did find one thing I hadn't considered: restriction in the ghetto intake tube. Took it apart and sure enough, there was a step down in the elbow that dropped the effective bottleneck to 34mm. That's right: thereby missing out on 4mm's diameter worth of effective throat area to transport precious O2. Doesn't seem like much, but I'm betting that it's enough to make her cough a bit, and perhaps artificially inflate the richness that these jets should provide. I've read several reports of similar carbs that simply didn't abide with an intake tube, and I'm betting that's why - not only is the velocity critical, but more importantly volume. Got a new Emgo filter on the way; similar design to the crappy one (chrome pod), but hopefully in a non-crappy variety. Emgo seems to be favored by some, so I'm hoping for a better build when it gets here. Got some new grips from Scrappy on the way too. ;D What can I say, I love riding but these hard plastic grips are just not the man-machine interface that they should be. Not expecting too much from the new grips, but they at least look like they'll be new and rubber-y, and that should make a noticeable improvement. But more to the point... Needing an alternate setup, I was at a bit of an impasse. Not enough clearance from the crossmember to just slap it straight on the carb (necessitating the ghetto intake tube in the first place). A trip to Ace found not much better in the way of off-label-usage plumbing bits. On a whim, I ran down the aisles on the other side of the store and found just what I needed: an 8' florescent light tube shield: thin, strong, yet flexible plastic tubing in exactly 42mm diameter. Woohoo! With this, I was able to make an internal coupler between the filter and 1/2 of the former intake tube's flexible rubber snout. (Hated cutting it, but the simple fact is that Ace has lots more.) End result: unrestricted filter on an effective 41mm ID running into a 38mm intake, that *just barely* fits, snug up against the back wheel mudguard. Straight neck of about 4" maybe total length between carb and filter. Should be no restriction here, and get some added velocity and reduced turbulence by going with the straight configuration too (on paper, at least). Emgo filter should be a straight swap upon arrival, barring any dimensional discrepancies. My intake probably is closer to 24mm for the most part, JR, but I was able to verify 23mm+ in measurement after rework. I'd seen that bit about the intake spacer before too, but hadn't thought to check mine yet. Sure enough, I found one corner had a 'crescent moon' overlap up to about 2mm at the fattest point. Had to go! I approximated your setup with a couple of machine screws through the stud holes on the intake & secured, using a radiused carbide burr as my weapon of choice. I was rather surprised to see the type of plastic used on this spacer; I expected something fairly supple and flexible that would absorb vibration, but it actually seemed to be a very dense formulation. Produced almost a chalk-like surface when ground on, reminds me of an older formulation I used to work with in an injection molding process. A graphite-powdered nylon mix, perhaps? It was eh...more than a few years ago. Anyway...plastic formulation ramblings aside... Got it bored out nicely, and some light sanding on the faces to help it tack (was a little cruddy). Thanks for mentioning that, I'm sure it will help matters. Got 'er started back up to find that the idle took a little bit more, telling me that the change did indeed increase the air side of the ratio as intended. Nice. Idle seems noticeably smoother. Checked the oil to find it a little higher than I expected. Having ran rich, I was a little unsettled by the thought of unignited fuel vapors potentially infiling the sanctity of my lube. So much so, in fact, that I went back out after dinner for a precautionary (and probably completely unfounded) oil change. Never hurts, right? The oil drained wasn't markedly gassy, at any rate, although it did seem a little thin for my tastes. Much more peace of mind with a fresh fill of Rotella 10-40 and a big fat squeeze of Lucas. Unfortunately too late for a test ride. Packed up and will give 'er a try tomorrow morning if weather cooperates. Supposed to be 25mph winds, so maybe not the greatest scoot-to-work day, but I'll likely ride anyway. The suspense'll kill me if I don't.
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Post by Evilgenius on Sept 28, 2011 6:41:13 GMT -6
Good news to report...rode to work this morning, performance was markedly improved. Temps were much lower, in the 50's, so the atmospheric leaning effect was more pronounced. This pretty much cinches it - I should be about a needle notch away from correct setting. Bummer is that I'll have to pull the tank to get at the carb, but I feel much better about that knowing that this should theoretically wrap things up. Will find out for sure tonight.
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Post by Evilgenius on Sept 27, 2011 20:17:19 GMT -6
As promised, the photos... The notch for Catalina/Majesty body style seat bolt access, check: One holey muffler, check: One shiny blue catch can, check: Closeup of ghetto intake tube, check: Gratuitous photo of how neatly everything fits behind the skirt, check check:
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Post by Evilgenius on Sept 27, 2011 18:01:17 GMT -6
OK...so, here's a little follow-up on that o-so-crappy air filter review. If you've got some free time and are feeling 'wordy', pull up a stool. Trying to do it all on a budget (virtually nothing, really), I set out to do a general air/jet/exhaust upgrade on my '07 Lifan 'Calalina' 150. After much frustration and silicon, I managed to get the air filter in temporary usable status. Fugly, but now serviceable. Of course, it would not fit straight on to the carb, necessitating an intake tube. And so, I set off to Ace Hardware. Can't say how much this place does for me in way of parts - I'm actually thinking an Ace sticker might find itself a home somewhere on the scoot. ;D Being a DIY type, with no real alternatives in town, Ace is quite literally "the place". A rubber boot, a PVC elbow, and a piece of 1-1/4" curved PVC later, I've got a nice intake arm stretching around the left side where the filter can get some fresh air. Filter socked right on there perfectly. Used a shiny exhaust hanger upside down as a foot for the arm. Should hold the carb up as a bonus. Would'a looked good too, if it weren't for the functionally necessary but aesthetically displeasing silicon all over it. Ultimately, that is of little consequence however; the filter pod is still safely behind the skirt when reassembled. I will be purchasing another (and hopefully much more sturdily-constructed) air filter to replace it, which will be similarly hidden. I'll know it looks better though. New jets came via Absolutely Scooters. Pilot swapped from 36->38 and main swapped from 105->115. Love the design on these! The main has an extra 1mm 'neck' above the threaded area below the cap, and the pilot just has an extended barrel, both for deeper reach into the float bowl. I can't say as I have any reason to think the stock jets were sucking the bowl dry beforehand, but it does make sense from an engineering standpoint IMO, and I like that. We can make him better than he was. Better...stronger...faster...The stock airbox was removed. Hated that damn thing anyway. Vent line's got to go somewhere, though! A while back, I came across one of those aluminum drink bottles in a shade of blue suspiciously similar to my scoot's paint job. I took this, and drilled two 1/8" holes in the cap, and stuck 2 weedeater fuel filters in the holes. The cap is hollow, so I just made 1 big vent hole to the 'inside' to feed both of them. The back (botttom) of the can was precisely drilled and a 10mm stainless quick disconnect was screwed in (the hose from the valve cover predictably followed). Some bigass hose clamps on the back frame, and I have a big phat catch can in matching color, vented and plumbed for ease of eventual dumping. Getting a first good look at my intake, I was pretty disheartened. The intake bore was forged. Poorly. This will not do! Took a carbide burr and took out the parting flash, with further finishing done by stone and heavy-duty nylon wheels. End result was an incalculably smoother bore wall, as well as an approximate 1mm increase in intake diameter. ;D Nothing wrong with that. Securely wrapped the elbow with good electrical tape as PM against dry rot-cracking due to the air box removal. I figured that if I was dumping this much more 'in', logic only dictates that the 'out' needs some help too. The header pipe was pretty clutzily welded; I'd previously removed the giant weld boogers, but took it a little further and drimmel-trumpeted the end this time. New exhaust gasket required, of course. Reduced back pressure was provided by drilling out the stock muffler rivets, removing the sleeve/cap, sawing off the pigtail 'straight', and putting a couple of gratuitous 1/4" drill holes on either side of the (now circumcised) pigtail, through the back wall of the muffler only. Riveted it back up with the rivet gun I inexplicably purchased several years ago and had never used, so that's always good too. Only downside to this I saw was that the front end rivet bottoms are trapped inside the muffler now. Oh well...can't win 'em all. A few miscellaneous tidbits while I was at it: the Majesty body types like this make seat bolt removal a huge PITA. This can be dealt with by clipping a couple of notches in the plastic to get a socket in at them, instead of wasting time and bolt corners wrenching. Once the seat's down, the notches aren't visible anyway. Some new hosing and a B&S fuel filter were added too, along with a fresh sidegapped NGK. And so, after reassembly...she fires right up. Beautiful! Started adjusting after warmup...set the fuel/air and took off for a test ride. Sound from the exhaust is OK. Little louder, but about as expected. More putt-puttier also, which I'm not sure that I like, as that indicates a 'dead spot' of flow in-between puts. Not cool. Will have to figure out if I want to keep this way, or put some bolts in the holes. (Hint: I've already got the bolts ready.) Performance not quite what I was expecting. Idle is OK, takeoff is OK, but cranking on the throttle to WOT produces a mighty unseemly bog. Midrange power is crap, and the engine seems to be 'fighting itself' to power through it. Once it gets to top end, it smooths out and seems to do OK, although top speed is not quite as good as previous (I'm attributing this to power loss as it's fighting through the bog). Swapped to a new, unmolested NGK just in case my side gap had somehow gone hiedously awry (it hadn't). Now to figure out exactly who's not playing nicely here... Examining my old airbox, I can't say as I think that there was much restriction there. My ghetto intake tube *might* drop the effective ID a little bit, but surely not enough to cause a throughput issue. It doesn't seem to be fighting for air, anyway. It's about as free-flow as free-flow gets. Ditto for the exhaust - theoretically, the restriction was mostly in the header pipe itself. Pigtail was only 2mm smaller than the header. My current thought is that the larger pilot is overlapping with the larger main in the mid-throttle and flooding it out. Experimentally, leaning the pilot seemed to help this a bit, but I'll have to pull the tank and/or carb to lean the needle on the main, which is more PITA. I haven't ruled out the exhaust, either. I may have got a little too enthusiastic with the drill and dropped back pressure too low, although I don't think this is likely. Possible though. All this being said, I'd welcome any opinions as to your professorial thoughts on the matter. Yes, I'll try and get some pics for all you scooter p0rn junkies. ;D
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Post by Evilgenius on Sept 11, 2011 21:41:35 GMT -6
Absolutely fair to the vendor - no complaints with them, really. They held up their end. When all's said and done, this is (will be) still a shiny and functional air filter to my door for a meager 8 simoleans and a little TLC with the silicone. One can't quite complain at getting that for less than a decent plate dinner. Still a respectable budget upgrade for sure. Especially if you have plenty of free time and a tube of silicone laying about the garage.
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Post by Evilgenius on Sept 11, 2011 16:58:33 GMT -6
Product: 42mm "Chrome" Pod Air Filter Vendor: Ebay vendor cenn2010: stores.ebay.com/cenn2010/_i.html?rt=nc&_dmd=2&_sid=1010406590&_trksid=p4634.c0.m14.l1581&_pgn=5Seems to focus on small odds and ends bike/scoot accessories. Lots of air filters and some sweet-lookin' hand grips, at what appear to be low prices. Price: $7.99 w/free shipping (A.K.A. "Dirt cheap") ;D Picture: (Not actual) Delivery/Packaging: Item was in a box, in bubble wrap, in gray plastic baggie. Cheapest of the cheap, but it got here just fine, in a reasonable time frame. Shipment was dispatched PDQ after payment. Blue plastic film to protect the shiny bits, which is cosmetically nice at least. Construction: Uber-soft chrome-y metal for the most part. Mesh and fiber for the filter area. Rubber snout. Quality: Big concerns here! Any unsuspecting scooterist that puts this on "as is" will be in for a world of hurt. Seals on this "filter" are so bad, you might as well just put a spaghetti sieve on your intake. Gaps at the snout/body mating surfaces and all the way around the bottom/top of the filter element/mesh. Snout rubber was warped to 38mm diameter on one axis (supposed to be 42mm round). Had to chamfer and buff the tip of my ghetto intake tube in order to get it started on so it would stretch back out. What makes it cool: It's cheap. It's shiny. It fits (after much coaxing). What makes it suck: It's cheap. So cheap in fact, that installing this without modification would likely result in grievous harm to your engine. Comments: Well, I've already got $8 sunk into it, and my jets are here too, so I'm going to make this work. A judicious application of sealant around the snout/body mating surfaces and the top/bottom of the mesh to plug the gaps should render it serviceable until I can get a better quality replacement. Not sure what I'll use to seal it up, but I'm sure it'll jump right off the shelf at me when I get to the parts house. ;D Conclusion: Don't buy one of these unless you're willing to trade your time and sealant to make it right. Spend a little more and get a better one if you want to avoid the headache.
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